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#1 |
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HYPER SS
Drives: 2016 Supercharged 2SS Join Date: Feb 2014
Location: Troy OH
Posts: 1,252
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Car running slightly rough after installs?
So I need some assistance or thought process.... Reason why I'm putting this here is because I'm forced inducted so some of you have done the same thing as I have.
1) I pretty much broke my car out of winter mode, had some colder plugs installed and gapped by Ted J. recommended plugs/gapping for my Maggie set up. I also installed a 1 size smaller pulley, and a E2-X catch can by Elite engineering. The car was running find last week from when my good friend installed it at the Chevy dealer he works at. Car sat until this morning. Granted it didn't quite fully warm up to optimal temps and I only work like 2 miles down the street. So didn't know. 2) This still has the same tank of 93 Shell octane with stabil since last September. 3) I have an appointment next Friday to get the car re-tuned for the new add ons that I have done. so I'm sort of babying it. 4) no check engine light or nothing, when I'm actual driving seems to be a faint stutter, but you can notice it at idle. you can feel the engine sorta stumble randomly. I don't know I guess its hard to explain. So any pointers would be helpful. I don't feel like there is a vacuum leak from the catch can. I would assume if there was it would be really bad and a possible check engine light.
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Ordered: 1/15/2016
2000 status 02/01/16 3000 status 02/29/16 3400 status 03/07/16 TPW of 03/14/16 4200 status 03/17/16 in transit! Delivered 03/23/16 2SS Hyper Blue | 6M | NPP | Mag ride | ceramic white Int. | Black out bow ties | P3 Gauge| Front splitter. | 6 pot upgraded brembo brakes. | Magnuson Supercharger/95MM pulley | Rotofab Intake | ZL1 side skirts | HRE FF04 wheels - Michelin PSS4 | ZL1 add ons rock guards and lift points. | AWE touring - resinated catback with link pipes. |
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#2 |
![]() Drives: 2016 1SS 6speed Join Date: Mar 2016
Location: IL
Posts: 527
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Get the old gas out of it. I just went through the same issue with my tuner. Old gas probably killed my O2 sensor. So he had to drain and fill the tank and slap a new O2 in it to finish tuning it. Couldn’t get nearly enough timing in it without the knock sensors pulling more because of the old gas.
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2016 1SS M6 P1SC Stg II 592rwhp/548rwtq (for now)
GForce Outlaw axles & driveshaft, TSP 2” LT’s, turndowns, RTS S71 drag pack with radials. |
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#3 | |
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HYPER SS
Drives: 2016 Supercharged 2SS Join Date: Feb 2014
Location: Troy OH
Posts: 1,252
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Quote:
__________________
Ordered: 1/15/2016
2000 status 02/01/16 3000 status 02/29/16 3400 status 03/07/16 TPW of 03/14/16 4200 status 03/17/16 in transit! Delivered 03/23/16 2SS Hyper Blue | 6M | NPP | Mag ride | ceramic white Int. | Black out bow ties | P3 Gauge| Front splitter. | 6 pot upgraded brembo brakes. | Magnuson Supercharger/95MM pulley | Rotofab Intake | ZL1 side skirts | HRE FF04 wheels - Michelin PSS4 | ZL1 add ons rock guards and lift points. | AWE touring - resinated catback with link pipes. |
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#4 |
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Drives: 2022 Lt1 A10 Join Date: Nov 2015
Location: clark, mo
Posts: 8,882
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Could have broken one of the plugs or could have a crack in the porcelain.
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#5 |
![]() Drives: 2017 1SS convertible Join Date: Feb 2018
Location: Oklahoma
Posts: 57
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I would say its tune and fuel related honestly. If this was after the tune it would lead me to think a mechanical issue with a vacuum leak etc.
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