08-17-2019, 09:46 PM | #43 |
Drives: '17 ZL1 Join Date: Jul 2016
Location: Fairmont, WV
Posts: 1,558
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I had another track day yesterday. The good news is, the power seemed normal again. The bad news is, I didn’t really come to any conclusions on the original problem. It's probably fair to say the lack of power was due to temperature/humidity/cooling, but whether it was beyond normal, I'm not sure anymore. It seems at least of few other people in the region were having similar issues.
For the changes... in addition to cleaning the air filter, I also checked the supercharger cooling circuit for air, which there didn’t seem to be any. I then upgraded the center heat exchanger as well as both auxiliary heat exchangers and then refilled the system and bled all of the air. The temperature was in the 80s yesterday at the track, and the car felt like it normally feels on a hot summer day. Power wasn’t 100% like it is on a < 70-degree day, but it still felt reasonably strong. For those who may be wondering...
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09-24-2019, 12:17 PM | #44 |
@Blackmamba_1LE
Drives: 2017 1LE Join Date: Jun 2017
Location: South Florida
Posts: 740
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Any feedback?
Idle temps???
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OG: Pray Perf FBO ET:11.5 @119 THEN:LT4 SC, E85 + Meth :10.6 @135 NOW: H/C Whipple 416ci
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