So I changed the oil last weekend I think and only drove the car a few times since then.
I was actually taking a HP Tuners log when it happened, but everything really looks normal, the only sign of the misfire is the rapid cycling, far higher than the normal switching frequency, that I drew an arrow too:
So it started misfiring right after a WOT pull from dead stop to 3rd gear.
Tomorrow I am going to try to look for for some valves to make a valve cut off to do a leakdown. I might just buy a harbor freight one if they have it though. I did also check cylinder #5 and #3 and they were at 182 psi and 178 psi.