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Old 09-12-2018, 04:35 PM   #24
TMS
 
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Drives: 2018 ZL1 1LE - HBM, PDR
Join Date: Jun 2017
Location: Rescue, CA
Posts: 324
Quote:
Originally Posted by 1LE Red Dragon View Post
How did you get the bolt back out this time? Cheater bar or drain the coolant and remove the fan assembly?

With all these troubles. Stock boost is starting to sound better and better every minute.
Easy. First, I got rid of the TTY bolt. Second, there was no adhesive under the head of the new bolt. Glad I went with the ARP crank bolt. I think that's why I didn't have any fits removing it. Those TTY bolts stretch to set them and then they are under constant tension (I guess that's why they are so difficult to remove). Just did the cheater bar and it broke loose fine. No heat. Easy Peasy.
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